 |
When hauled out in the Fall of 2002, the rudder was not in good
shape. It was evident that water intrusion into the core was the
cause of the problems evidenced by weaping stains near the bottom
of the rudder. This is what the rudder looked like in November 2002:
(click on images for higher resolution view).
|
 |
The rudder was removed (a bit of a project in itself as the thing
is not light), brought home and some 1-1/2" holes drilled
to allow the unit to initially dry out. It was kept in a warm place
(next to the hot water heater) for about 2 months, and then the
a brought back outside on a frigid morning for an appointment with
the angle grinder. All of the holes that had been drilled through
the skin were flared to a 10:1 angle in preperation for re-laminating,
and other bad spots on the rudder ground back to good glass or core
...
|
 |
After this was done, the rudder was brought back inside, put under
heatlamps and dry compressed air at low pressure blown through the
rudder for about a week. This was done to help flash off any residual
styrene inside the rudder and to finish the drying process. At the
end of this process, the air emerged from the rudder odor-free indicating
that at least along the paths that the air was able to take, the
rudder was substansially dry. 30 oz fiberglass cloth was then laid
up ...
|
 |
Then the source of the problem was dealt with. Most rudders that
get saturated leak water through the joint where the rudder shaft
joins the body ... its a tough connection to get right, and to keep
intact given the stresses that the joint takes under sail. My approach
to solve the problem was to grind back a half-V shaped notch about
1/2" deep around the top of the joint, and then roughen the
stainless inside to permit maximum epoxy adhesion once the repair
was attempt.
|
 |
A vacuum pump hose was hooked up to a hole on the leading edge
of the rudder, and other remaining holes in the rudder sealed, permitting
expoxy to be drawn down along the shaft. The vacuum was applied
and an initial set of epoxy poured into the notch and drawn down.
This was quickly followed by chopped strand glass to stiffen the
joint area and left to cure under the lights.
|
|


|
Additional spots were fixed, including the holes on the leading
edge which was filled and taped, and fairing the job began using
high-temp polyester resin that is rated for below waterline use.
|
 |
Then it was time to put some barrier coat (Interprotect 2000) on
...
|
 |
And to rehang the rudder ...
|
Easy as pie! Will it hold up? Check for an update in the Fall of 2003.